Xinjiang Oil & Gas ›› 2022, Vol. 18 ›› Issue (1): 80-85.DOI: 10.12388/j.issn.1673-2677.2022.01.013
• OIL AND GAS DEVELOPMENT • Previous Articles Next Articles
LIU Kaixin1,ZHENG Weijie1,DAI Liya1,PAN Liyan1,ZHANG Long2,CAI Guoqing3
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刘凯新1,郑伟杰1,戴丽娅1,潘丽燕1,张拢2,蔡国清3
作者简介:
Abstract: The reservoir of Triassic Karamay Formation in well block X was developed by vertical well water injection in the early stage. As a result,the injection effect was insignificant,the production declined fast,and the overall recovery factor was low. In order to fully produce the remaining oil resources in the block,the original development mode was changed to horizontal well volume fracturing in 2018. The first well executed in 2019 was subjected to annulus fracturing using coiled tubing with a bottom packer,and the initial production of single well after fracturing was increased by 11.5 times compared with that of a vertical well. That validated the feasibility of increasing the production of horizontal wells. In order to satisfy market demands,field tests have been carried out in this block since 2020. Annulus fracturing using coiled tubing hydraulic jet has been gradually substituted by staged fracturing with bridge plug perforating,and the fracturing fluid has been changed from guar gum gel to guar gum slick water. A set of low-cost volume fracturing technologies has been developed. The application results show that: ①the 13 horizontal wells put into production using different technologies have all achieved design productivity; ②uneven fracture initiation can be improved by using bridge plug staged perforating + uneven distribution of perforations; ③insufficient sand-carrying capacity of guar gum slick water can be made up for by increasing the injection rate to ensure safe sand filling during field treatment; ④low-cost volume fracturing technology can reduce the fracturing cost by nearly 30%.
Key words: uneven distribution of perforations, proppant placement, conglomerate reservoir; low-cost exploitation
摘要: X井区三叠系克拉玛依组储层前期为直井注水开发,注水受效不明显,产量递减快,整体采收率低。为充分动用区块剩余油资源,2018年将原有开发方式调整为水平井体积压裂开发,2019年实施的首口井采用连续油管带底封拖动环空压裂,压后单井初期产量较直井提高11.5倍,验证了水平井提产的可行性。自2020年起为适应市场环境需求,在该区块开展矿场试验,逐步将连续油管水力喷射环空压裂转型为桥塞射孔分段压裂,压裂液体由胍胶冻胶过渡为胍胶滑溜水,形成了一套低成本体积压裂技术。应用效果表明:①采用不同工艺投产的13口水平井均达到设计产能;②使用桥塞射孔+非均匀布孔方式可改善起裂不均衡的问题;③通过提升排量可弥补胍胶滑溜水携砂能力差的不足,保证现场施工安全加砂;④低成本体积压裂技术可节约压裂成本近三成。
关键词: 非均匀布孔, 支撑剂铺置, 砂砾岩油藏, 低成本开采
CLC Number:
TE357
LIU Kaixin, ZHENG Weijie, DAI Liya, PAN Liyan, ZHANG Long, CAI Guoqing. Exploration into and Practices of Low-Cost Volume Fracturing in Well Block X[J]. Xinjiang Oil & Gas, 2022, 18(1): 80-85.
刘凯新, 郑伟杰, 戴丽娅, 潘丽燕, 张拢, 蔡国清. X井区低成本体积压裂技术探索及实践[J]. 新疆石油天然气, 2022, 18(1): 80-85.
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